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authorLuke T. Shumaker <lukeshu@lukeshu.com>2024-11-29 13:55:29 -0700
committerLuke T. Shumaker <lukeshu@lukeshu.com>2024-11-30 10:33:16 -0700
commitcda33a489898c18024823b4d4b6e5e0c3b2de24a (patch)
tree4fd3dc9af57e9451df072788cef20c8bc129db3f /cmd/sbc_harness/config/tusb_config.h
parentfb2322993268c0d8441971446a9c716b28545a7b (diff)
Don't use TinyUSB BSP
I guess the BSP is only meant for demos, and doesn't play nice with a larger project. Notably, board_init() re-initializes the UART hardware, causing weird glitches.
Diffstat (limited to 'cmd/sbc_harness/config/tusb_config.h')
-rw-r--r--cmd/sbc_harness/config/tusb_config.h14
1 files changed, 1 insertions, 13 deletions
diff --git a/cmd/sbc_harness/config/tusb_config.h b/cmd/sbc_harness/config/tusb_config.h
index fc963ac..a27c841 100644
--- a/cmd/sbc_harness/config/tusb_config.h
+++ b/cmd/sbc_harness/config/tusb_config.h
@@ -36,18 +36,6 @@ extern "C" {
#endif
//--------------------------------------------------------------------
-// TinyUSB Device (TUD) initialization for rp2040-based boards
-//--------------------------------------------------------------------
-
-// Which USB port to use for the RootHub.
-// The rp2040 only has 1 port, so it's gotta be port #0.
-#define BOARD_TUD_RHPORT 0
-
-// RHPort max operational speed.
-// Use OPT_MODE_DEFAULT_SPEED for max speed supported by MCU.
-#define BOARD_TUD_MAX_SPEED OPT_MODE_DEFAULT_SPEED
-
-//--------------------------------------------------------------------
// Configuration: common
//--------------------------------------------------------------------
@@ -72,7 +60,7 @@ extern "C" {
#define CFG_TUSB_MEM_ALIGN [[gnu::aligned(4)]]
#define CFG_TUD_ENABLED 1
-#define CFG_TUD_MAX_SPEED BOARD_TUD_MAX_SPEED
+#define CFG_TUD_MAX_SPEED OPT_MODE_DEFAULT_SPEED
//--------------------------------------------------------------------
// Configuration: TinyUSB Device (TUD)